Current number:
975983
Any other previous number(s):
BR coach 12162
Notes:
Scrapped - Derby RTC on site by T. Hill 11/85
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All Sightings
| Location | Date | Observer |
|---|---|---|
| Derby RTC | ** *** **** | Leslie Wild |
| Derby Loco Works | ** *** **** | Simeon Gaskell |
| Wolverton Works | ** *** **** | Carl Watson |
| Mickleover Test Site | 1984-03-03 | Brian Cuttell |
| Crewe | 1983-04-02 | Duncan Elsey |
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Comments
The following comments have been left on photos of this vehicle. To reply, just visit one of the photos.

975983
9 December 2007 - Ben Williams
Certainly looks like its undergone some stress (!) but can anyone elaborate please?
975983
10 December 2007 - ian saunders
judging from the scuff marks and the fact that it is recorded as a stress measuring coach it would appear that this vehicle has spent some time on its side, probably to test the ridgidity of the design. It may also have been used for training purposes
975983
10 December 2007 - barry brainfunk
i think they filled it with yuppies and told them something stressful
975983
10 December 2007 - Andrew Humphries
I believe that this was one of the coaches damaged in the crash at bushey - 1980
975983
10 December 2007 - Bill McTavish
Hmm a lot of speculation - anyone got any facts?! I think I could have probably guessed it had been on its side!
975983
11 December 2007 - Andrew Humphries
Just to update. 12162 ( 975983 ) was involved in the derailment at Bushey, it was the 4th vehicle in the train (20.25 Euston to Manchester Piccadilly on the 16th February 1980).
It was 1 of 3 coaches that over turned in the accident. the sheeted over area on the side is where it landed on a detached bogie.
It shows the strength of the MK3 Coach, the train was going at 100mph when it derailed. Taking out 4 sets of overhead gantries as the train progressed.
Of the estimated 150 passengers on the train 48 were injured none killed.
If you want more information on the accident the link below is to the official report.
http://www.railwaysarchive.co.uk/documents/DoT_Bushey1980.pdf
The three overturned coaches were taken to Wolverton for tests to measure impact and damage sustained in the accident, after assessment I believe that none re-entered traffic.
975983
11 December 2007 - Ben Williams
Interesting Andrew, thanks. So presumably it received its departmental number while in its post-crash state to reflect its role as an assessment vehicle. Seems a bit odd to bother renumbering a coach that is essentially going for scrap (it would never happen these days!) but there it is. Another departmental story uncovered!
975983
11 December 2007 - Simon Bendall
12162 was originally taken into departmental stock for fire testing, as part of a series of tests on condemned rolling stock following the 1978 sleeper fire which killed 11 people. With Mk.3s the then current coaches, it was obviously useful to retain it for this, even if written off.
The stress tests came much later, following transfer to the Research department (it was originally M&EE operated, ADB prefix). If I recall correctly, it was cut into sections for this and then placed under load.